no pics???? Need to see it to believe it.![]()
no pics???? Need to see it to believe it.![]()
Well, finally got this out from under another one and back on a rack. Neil and I got the tank out and redid the lines that got messed up 2 years ago and pretty much soured me on this thing til recently. So redid the lines and moved the filter further downstream out of the way. Now all the lines are routed correctly and hopefully no more leaks. I need to order some -8 and -6 hose ends to finish under the hood too. Then finish up the brakes on it as well. Pics soon.
Last edited by NXcoupe; 12-16-2019 at 04:15 PM.
Gonna be a cool car when its finished. The old 4 eyed cars have really grown on me over the last few years. And a coyote to boot!
You guys have made good progress in the last couple weeks.
1992 Mustang LX Coupe, 302, PA C4 and On3 70mm.
1993 Reef Blue hatch, 347, 3550, and a kit.
1992 Gould GT project...
Here we are, all these years later. I am going to finish this car and sell it. It has a lot of mixed emotions with it, I really just want it gone. This was supposed to be a 6 month turn and burn, and here I am 8 years later, and it still isn't finished. That changes now. Neil has been instrumental in helping me get this thing to the point it is now. I go out and work on stuff through the week and on weekends, with the goal being to have it for sale at the spring swap. The big hold up now is the steering shaft from Maximum Motorsports. I ordered it in December, and still don't have it. I called today and they said possibly in three weeks.
I hated the roll cage, just hated it. The passenger side interior quarter panel plastic was in really bad shape, the driver's side wasn't as bad. I bought a nice one, but the old one just would not come out. Turns out the bar was closer on that side, and the panel just would NOT slide out no matter how I tried it. I wasted a lot of time on it and finally, out came the sawz all. I sliced it off the mounting plate flush, and then used a come along to pull the bar over out of the way. I got the old panel out, new panel in, and then released the strap. I put my antique port a power in and positioned the bar to its new location after I had ground the plate down and the bottom of the bar. I laid a great bead on it and called it done. Since then, I had to pull the panel out AGAIN, but this time, it slid right out because of the new location.
NOTE: The panels look like two different shades, but they are not. Both are out of a 91/92.
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I cut out the kicker bars, as they were angled forward and limited the movement of the front seat rearward. I figured if a bigger guy wants to own this, he would want the seat to move back. So I cut them out with the sawzall as well.
The to front down bars also bugged me because they were bent in to far to clear the armrests. I like it to be about 1/4" away from the armrest, these were more like an inch, maybe a little less. This caused the bar to smash the side of the factory seats. I decided to install swing out kits on both front down bars. They really weren't too bad to install and they look fantastic, especially laying in the back hatch area, yuk yuk.
We prepped the interior to protect it from grinding and welding sparks, and I set to work with the cut off wheel.
Lots and lots of measuring before cutting and ended up with this! I really like this setup a ton better.
Everything painted up with Rustoleum Hammered Black. It matched up really well.
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Last edited by NXcoupe; 03-08-2023 at 09:36 PM.
Next up I needed to make a radiator hold down that would be kind of neat and one off. I bought a tool that allows me to bend steel round stock and square tube. I think it turned out really nice.
I needed to mount the combination radiator surge tank and power steering reservoir somewhere, and we had settled on the driver's inner fender area, but while admiring and critiquing my work, I thought, what if? and then I set out to add onto the radiator hold down and mount the tank off the radiator.
I bent the rod, and then set about getting it made. Jason was kind enough to weld tabs onto the tanks for me, since I still cannot weld aluminum, well, for now.
I really like how it turned out. It left the driver's side nice and clean looking now. This is where it belongs.
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We are starting to get down to the short list, so I moved onto the top of the door moldings. We also replaced the damn quarter windows, which not being able to get the panel plastic out of the way made it a real bitch! These moldings were just dead looking and had some chips out of them, so on went the new and improved!
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lookin good!
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